Modeling – The Present – Version 5, The Casper Layout
This page shows current construction on the layout. The most recent entry is at the top, and they get older as you scroll down. Every now and then, when the page gets too long, I'll move everything into the appropriate link just below. Enjoy!
23 November 2024
After the operating session I took a couple days off from the layout. Then, because I didn't feel like doing anything else, I began staining the ballast on the mainline in Casper on the 26th of October. The very white ballast to the right just didn't look right. Staining it gave me what you see on the left.
When they showed up a few days later, they looked like this:
Idiot seller didn't pack them properly for shipment. By the time they arrived, nearly all the stirrup steps had been broken off by the jostling in transit! Seller did refund about 25% of the purchase price, but still...
Now what would have taken maybe 90 minutes of prep time to get them on the layout (change trucks and weather) will now take three to four hours with the repair work I have to do.
Unlike the hoppers and the locomotive I bought early in October, this one was fine. I programmed a motor decoder to 5502 (the Bluelines are dual-decoder locos) and installed it. If I'd had a decoder with a harness everything would have fit fine, but because the decoder didn't have a harness, it sat too high up for the tender shell to go back on. I shaved down the spacers that mount the sound decoder to the bottom plate in the tender, and then the shell popped right back on. Here's the modified tender before adding the shell:
Just yesterday I got around to re-lubricating 5502, and suddenly the chuffing sound was missing! All the other sounds worked fine - bell, whistle, blow-down, etc. With a bit of research I discovered that the chuff sensor sometimes fails on these locos. Hopefully BLI has a replacement I can purchase and install. Meanwhile I have a loco with intermittent chuffing. But I got the chassis and mechanism lubed and tuned, so it runs just fine, even if it sounds a bit funny. Here it is:
I posted my latest layout update video, number 60, on November 3rd.
That loco with the bad driver set I bought in early October, which I renumbered to 5506, was acting a bit funny during the operating session. I need to do some additional work on its mechanism. That's slated for sometime over the next few weeks. Here it is still coupled to the reefer train it was assigned to for the session:
Here's a shot of the trainset power pack I was using to power the staging occupancy detectors. It doesn't have quite enough oomph! to power all 18 of the detectors, so after about an hour it goes into thermal shutdown and won't turn back on until it cools off. It's going to be replaced during the next few days with an MRC powerpack.
I left Powell for a couple of weeks for other projects, but the a couple days ago I got back to it. I cut all the subroadbed to take the line from Powell to Vocation, and hopefully around the turnback curve on into Cody. Here it is leaning against the wall in the garage. This will require new benchwork to support everything under Thermopolis and Wind River Canyon.
By far the biggest project I tackled so far this month is ballasting the mainline from the middle of Casper all the way to Powder River. That wasn't on my list of things to do, but since I'd stained all the existing Casper mainline ballast (well, almost all of it - I still have to a couple feet of the far east end), I just decided to add more ballast. I've been wanting to ballast the track through the scenicked area towards Powder River, so I decided now was the time.
Here's the first stretch of new ballast on November 10th:
Yeah, it's that white ballast again. I'll just stain it like I did the rest.
After getting the ballast all the way to the Powder River turnout I went back and began cleaning up the stray ballast on top of the ties and against the sides of the rail. That's when I found out two things - my grooming job wasn't all that good, and in many spots I didn't use enough glue. As I scraped away ballast in some spots it exposed loose ballast underneath. When I vacuumed up the ballast I'd chipped loose, in a few spots I had holes where the underlying ballast was sucked up as well! It took hours and hours to scrape away the stray ballast and then repair the holes.
Here's the brown ballast west of Casper. The darker spots are where I did some ballast repair. I made sure to use plenty of glue on these spots!
I needed a very small scoop to place the ballast in the repairs without dumping it all over the place, and I found exactly what I needed in, of all places, a vape shop. Apparently this small scoop is used by marijuana smokers in some fashion, but it turned out to be perfect for delivering small amounts of ballast in just the right spots.
Over the last couple of days I posted a two-part compilation of Runcam 2 videos taken on the layout.
24 October 2024
On October 3rd I posted my latest layout update video.
I bought another BLI Mikado on ebay, from a seller who said it was "like new." Well, it was clean, but it moved about a quarter of a driver revolution and lock up solid! You have to be very careful buying on ebay! The problem turned out to be that the front driver set wouldn't stay in quarter. One of the drivers just spun on the axle! Fortunately I have a damaged unit I use for spare parts, and I was able to use the front driver set from that to repair the loco. I re-numbered it as 5506. We used it in the operating session a couple days ago, but it needs a bit more work before it's completely satisfactory.
Work on the layout slowed down to almost nothing for several weeks, as I turned my attention to preparing for the Operating Session coming up later in the month. As part of those preparations I trimmed off the extra braces from the decades-old tunnel portal I had for Wind River Canyon, and set it into place. With the light shining into the hole, you can see some of the pink foam at the far back where the track curves away to the left.
I didn't have time to take any photos of the session, but we had a record turnout! Ten people showed up. The train room was crowded!
Things went okay but the layout didn't perform as well as I wanted. A few locos and cars need some work before the next session - if there even is one. More on that last statement in the future.